摘要:
针对钒渣钙化焙烧温度过高导致物料烧结、回转窑结圈的问题,采用提高焙烧气氛氧含量的方法,强化焙烧动力学条件,降低焙烧温度,并进行了富氧钙化焙烧实验室试验和工业试验研究。研究结果表明:在控制尾气氧含量12%~14%的情况下,焙烧温度从富氧前的920~940℃降低到富氧后的870~885℃,降低了约50℃;工业试验过程中,物料绝大部分为粉料,回转窑运行正常,焙烧获得的钒转浸率为89.58%。采用钒渣富氧钙化焙烧技术,解决了焙烧设备不能正常运行的问题,实现了钒渣不配尾渣直接焙烧。
关键词:
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钒渣 /
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钙化焙烧 /
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富氧 /
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焙烧温度
Abstract:
According to the problems of sintering and ringing in rotary kiln caused by the high temperature during roasting the vanadium slag with calcium,the roasting dynamic conditions were enhanced and the roasting temperature was reduced by increasing the oxygen content in the intake air.Both of the laboratory and industrial experiments were conducted,and the results show that roasting temperature,920~940℃ before the experiments,decreases to 870~885℃ after adopting the oxygen-enriched roasting by controlling the oxygen content in the outlet air in the range of 12%~14%.During the industrial tests,most of the clinker exists in the form of powder and the leaching rate of vanadium is 89.58%,coupled with normal operation of the rotary kiln.The operation problems of the roasting equipment are resolved.Meanwhile,roasting vanadium slag without tailings is realized by employing the oxygen-enriched calcium method.